|
Post by peterberg on Nov 23, 2023 12:31:19 GMT -8
Years ago, I tried a tapered riser Travis Armstrong posted about it. donkey32.proboards.com/thread/3379/tapered-riser-batch-box-coreThe thing seemed to work quite well, work on this slipped into the DSR2 concept eventually. But the notion of a shorter riser stayed in my mind. Now that the DSR3 design is sort of established, one of its important properties is the maximised burn rate. Plus no steel in the firebox itself and a low profile. A bit complicated design to build first time, I admit that. In line with the tapered riser, why not a riser that would be as wide and deep as the width of the firebox? And much lower, actually it leans on the notion that the volume of the normal riser is implemented in a compact way. I have been busy with building, changing and testing since November 6th and I have to say, it looks like it is going to work. The firebox itself is according to the established recommendations, bar one aspect: the port. This is quite a bit narrower, it's a 60% one, formula 2.1B high and 0.4B wide. B being the base number that is used to calculate most of the meaurements of a batchrocket. The port has been a number of sizes, this size seems to work best. Riser is as wide as the firebox as I mentioned, and has a square shaped floor. Now this didn't work as intended, there was just a straight flame from the port and nothing else. No double vortex nor even a fire fountain. So in the small development model I introduced a liner on four sides but not any higher than the port. Everything above that is wide again. Not much above that, mind you, the total height of the riser is 5B instead of the recommended 10B. The air inlet is entirely through the door frame, in fact it's the same door as I used for the DSR3 development model albeit I modified it to fit the new core. So no P-channel, floor channel or whatever. So far, with a riser top that's closed off partly with two strips of potter's shelf leaving a gap in the middle of just 110% of the system size csa. The system is one with a 130 mm diameter chimney pipe, just a little bit larger than 5". So it worked, but making the end port wider or narrower only resulted in more instability as it came dangerously close to overfuelling every time it was run. Today I solved this, just by shifting the gap in the middle of the riser's top to the front side of it. Now it's not a converging thingy anymore, unlike a De Laval nozzle is doing. As I see it, there are two competing streams now, one that is able to go straight up and one that is rising at the riser's back wall. That last one is arriving at the gap slightly later and is interfering with the straight stream. The net result is a burn that won't race through, exactly like what the DSR3 is doing. It's still early days, the end gap is initially set on 100% now. It might be a bit tame for my liking so at some point I'll try a larger gap. Pictures are on their way, will be implemented in due course. Another event: my trusted Testo 330-2 died quietly some time ago, repairing would be very costly with more repairs in the not-too-distant future. I pondered over giving testing up altogether and let this Shorty idea untried. But oh well, a pensioner has to have a hobby and hobbies are costing money so I bought a new Testo gas analizer, a T-300 this time around. It's getting used to, works a little different as compared to the old one but the new software could be run on the old small laptop I used for years for this purpose.
|
|
|
Post by peterberg on Nov 24, 2023 9:50:14 GMT -8
First a couple of pictures, just to show what has been done so far. The setup is of two slightly conical barrels, with the open tops connected to each other. Both barrels were old ones and quite battered and didn't fit together well. So every time I wanted to change something new aluminum tape had to be applied to close it up again. The core is built in a steel box which is fixed to the lower barrel. The exhaust hole is situated below the core. Higher up the steel rod is visable where the steel box is welded to. There's a second bar on the top front and also welded to the box. The core is built partly out of old 30 mm refractory pieces, some new 15 mm pottery shelves and leftovers of 10 mm shelves. All around is 25 mm superwool, even under the firebox' floor. Next picture shows the riser box, insulated as well. The door frame is bolted to the steel core box, any crevices between steel and refractory are sealed with superwool. Later on, I added roughly 30 mm to the height of the riser box, that's it. As is clear, the riser is very short. And here's the complete setup, very ugly but functional. The door and door frame are the same as used for the DSR3 development, only the top door has been cut off. Air is supplied through the single inlet in the door, feeding into the door frame and streaming into the firebox through the slits in the top half of the door frame. Here's the liner inside the riser box, done in 25 mm superwool. It shows a bit higher than the port, I took the surplus off later. There wasn't a difference that the Testo could measure so I am confident upto the port's top will be enough. Of course it could be done in any refractory material, the wool was the easiest since the hired wet saw was returned at the time.
|
|
|
Post by peterberg on Nov 25, 2023 8:44:32 GMT -8
The height of the riser box has been at 4.5B, 5.5B and is now on 5B. The centered end port has been at 80%, 90%, 100% 110% and 120% of chimney csa. The results of running the shorty with all those openings, one by one, made clear that instability was higher with the smaller ones. Sometimes a really good one came along and most of the runs would pass the EU conformation test for the parameters I am able to measure. The diagram from November 11th was notably nice, maybe due to the fact most of the refractory parts weren't dry yet. Some others were downright not good, racing through and producing a large CO peak. Oxygen level went very low in a number of instances, although not all the time accompanied by the CO peak. The one from November 20th was remarkable in that aspect, oxygen went down to 4.5%, a sure recipe for disaster in the past. Most of the test runs were done with a 60% riser port and a 110% end port, centered still. Until I got the notion that the centered end port would probably act as a convergent opening, getting higher speed and lower pressure. The narrower the port, the more speed. So I tried something similar to the DSR3 end port, the effect of that one is completely opposite, the narrower it is, the slower the burn. To this end, I shoved the opening towards the front of the core and tried a 100% opening. The first testrun with this configuration was done on a very windy day with many gusts, it shows. But on the other hand, it looked quite good, the door was closed all the time and I did nothing to interrupt the way it behaved. End port 100% of chimney csa. This went very well, despite the wind gusts it was all within EU parameters. This happened to be also a warm start and bottom lit, unlike the other runs which were all top lit. Next day, November 24, a calm day, firebox loaded with 2.8 kg of soft wood, door closed at the 11 minutes mark. This happened to be the best run to date, ran very calm with nice numbers. Next goal: trying slightly larger and smaller openings, I am confident this is the way forward.
|
|
|
Post by martyn on Nov 26, 2023 0:17:26 GMT -8
Have you tried the riser with just a full size open top, I tried that with a vortex (Trevs style) in a single barrel with no form of riser at all and it worked but I did not pursue the idea at the time.
|
|
|
Post by peterberg on Nov 27, 2023 2:45:37 GMT -8
Have you tried the riser with just a full size open top, I tried that with a vortex (Trevs style) in a single barrel with no form of riser at all and it worked but I did not pursue the idea at the time. As a matter of fact, I did. It worked but the burn didn't progress well. It burnt faster and faster and eventually the CO went through the roof. Typically for a burn that ran out of hand, I'd say. In fact I did two test runs: one with a 70% riser port and the other with a 60% riser port. Results are very much alike, so I ditched this open top idea very quickly. See the contrast with two recent tests, three days ago and yesterday night, both with the latter end port, 100% and 105% chimney csa respectively. Both show the same behaviour, load and same fuel, the latter one ran slightly faster so O² is a bit lower logically. Lowest O² is 8.7% and 7.5% respectively. I am in the tuning phase now, so to speak. Getting there, slowly, but I won't be hurried. Next run I will be using hardwood scraps.
|
|
|
Post by foxtatic on Nov 27, 2023 7:51:47 GMT -8
Hey thanks for the preview of the new design, Peter. I assumed it would be another ceiling port style building upon the DSR3 design! What benefits are you hoping for on this one? Just smaller than a typical batch box riser without the "folding-over" of the DSR2?
|
|
|
Post by fruitbat on Nov 28, 2023 2:53:30 GMT -8
Wow, really exciting stuff! Not only is this new core lower in height, but also looks like it can be built at far less cost- Fewer refractory components needing to be purchased, and only simple, widely available ones at that.
It always amazes me how many people are still building J-tubes, with their requirement for constant feeding and huge bulk. A simple low cost design like this is just what is required to make the batch principle accessible to all.
I can envisage applications in cooktop stoves where low height is important. And even with this core placed in a large bell, it could be ppositioned comparatively higher up, at a more ergonomic height for lighting and feeding...
Thank you so much Peter for sharing your progress, it's thrilling to be watching the future take shape!
|
|
|
Post by peterberg on Nov 28, 2023 7:34:19 GMT -8
Hey thanks for the preview of the new design, Peter. I assumed it would be another ceiling port style building upon the DSR3 design! What benefits are you hoping for on this one? Just smaller than a typical batch box riser without the "folding-over" of the DSR2? The main benefits are the lower cost to build this core, the lower profile, no steel parts in the firebox itself and the opportunity to use a core that's regulating itself to some degree. The flip side of the coin is a more complicated air inlet design and a deeper core size. That last one could be mitigated by building it as a sidewinder. Mind you, the height profile is even lower than one of the shoebox designs.
|
|
|
Post by peterberg on Nov 28, 2023 7:36:28 GMT -8
Thank you so much Peter for sharing your progress, it's thrilling to be watching the future take shape! Thanks for the compliments. Please don't hold your breath, the devil is always in the details.
|
|
|
Post by peterberg on Nov 30, 2023 2:38:27 GMT -8
Sometimes, results tend to be very surprising, leaving me puzzled about the possible cause. Three days ago, November 27, I planned to do a testrun using hardwood because I wanted to see the differences as opposed to using softwood. I had a small crate of old oak scraps lying around, so I decided to use that. Very old oak, very grey on the outside. The resulting diagram turned out to be very different, even disappointing, to say the least. Oxygen level came down very late in the burn, CO came up high and early. In general, to the eye it didn't look like a bad burn at all. But the Testo analyzer registered lots of CO, a mediocre burn. Nothing was changed in the configuration so I suspected something might be wrong with the fuel. I let it sink in for a day or two and decided to use some healthy, unused, beech logs for a reference burn. It turned out to be necessary to split those logs up, since they were too large for the tiny firebox of the 130 mm (5.12") system. I could cram in a mere 4 kg (8.82 lbs) of bone dry, nice hardwood. The burn progressed quite good, not as slow as the other one. This happened to be a cold start and top lit, as standard just to eliminate temperature and lighting differences. This diagram looked much better, although the CO start peak wasn't very nice. Surprisingly, although the CO was on the high side of things, with both runs, the white filter of the Testo came out as just light grey. Is there a trade-off between soot and CO? I've seen it before, not as pronounced though. In order to check the condition of the old oak planks, I'd burn another load in our own red bell heater yesterday night. Just the regular evening fire, uptil now we didn't have fires in the morning. Now this burn turned out as very sluggish as well, but no smoke stench at all outside. So, the not-so-good results are probably due to the second rate fuel. Next stage: enlarging the end port to 110% of chimney csa and see what happens. Softwood species first, those are free, hardwood have to be bought. Just one 4 kg load left of the better species.
|
|
|
Post by peterberg on Dec 3, 2023 9:29:47 GMT -8
Still eliminating port configurations in order to find out what the stable ones are. As I mentioned, I enlarged the end port to 110%, firebox port still at 60%. Fuel 3.3 kg (7.28 lbs) softwood, wind force 2, door closed at 10 minutes. The results were not good, the core failed to limit the burn rate sufficiently. To make matters worse, the white Testo filter turned to pitch black. New day, new chance. I reasoned I crammed the firebox too full last time so I tried another load. Softwood again, 2.5 kg (5.51 lbs), cold start, wind force 2, top lit, door closed at 11 minutes. I kept loads of air at the top and the sides, maybe I could prevent overfuelling that way. And yes! No overfuelling although not a good burn either. Now the burn refused to come up to speed at all and the diagram looked stable but shitty in the real numbers department. After a day of grumbling and brooding over it, waking up at night a couple of times, I concluded this wasn't the way forward. The darn thing had to do its work well with a plethora of fuel arrangements and species otherwise I'd better ditch the whole idea. So, the end port was rearranged to 90% of chimney csa, and I mimicked the fuel load of the day before. Most of the other configuration details being the same, even the weather gods played ball. This went much better, bar one spot. Where the CO went up in a sharp smallish peak I added two pieces of fuel. With the idea I might be able to provoke it into an overfuel situation. But to my pleasant surprise it didn't, it corrected itself within two minutes and went on the exact right way. So, in order to repeat this latter behaviour without the peak, today I loaded the thing again with a bit more fuel 2.9 kg (6.39 lbs) and somewhat more densily packed. Still lots of room above the fuel and behind it. This time the burn progressed very calmly, I refrained from tampering with it and it payed off. CO went down and stayed there for quite an extended period. O² went down nice as well, efficiency comfortably high as a consequence. The Testo filter happened to be just lightish grey, not very dark as the day before. Progress has been made, next run I'll take my chances with the last portion of hardwood species available in-house.
|
|
|
Post by fruitbat on Dec 3, 2023 14:55:21 GMT -8
Watching with interest!
I'm trying to understand the physics of what is happening in this 'shorty' riser- As well as the turbulance caused by the firebox port and the 90 degree change of direction of the gas stream, is the shorty riser acting as an expansion box, with the end port providing back pressure/resistance to moderate maximum flow to keep the overfuelling in check?
|
|
|
Post by peterberg on Dec 4, 2023 5:00:41 GMT -8
That's the general idea, yes. How this happens in reality is anybody's guess but as long as it works, who cares?
|
|
|
Post by fruitbat on Dec 4, 2023 10:59:08 GMT -8
Too true, let's hope it turns out viable...
|
|
|
Post by independentenergy on Dec 5, 2023 6:21:04 GMT -8
Hi Peter, I was looking for a core with these characteristics, when you have a good enough version I could build it. I have a construction with a cooking plate and a small bell, connected to a 10 meter chimney in 150mm insulated stainless steel. I opened a post ( donkey32.proboards.com/thread/4055/replace-tube-batch-box ) for some advice on which core to install since I demolished the jtube that powered the system, this design is compact enough and not too much else for a cooking plate. but I can only build with hard refractory bricks, no insulation except on the outside.
|
|